Blade Cost Reduction
- Led cost reduction trials for high cost custom blades used in APM machines, with lower cost alternatives, projecting $20,000+ in annual savings.
- Conducted operator interviews to assess blade failure modes, replacement frequency, and operational challenges.
- Tested multiple blade assemblies focusing on durability and compatibility.
Rework Process Optimization
- Conducted a comprehensive analysis of the membrane rework process across production areas identifying inefficiencies in documentation, traceability, and communication.
- Interviewed operators and teams lead to understand of pain points in the DMR (Defective Material Report) process, revealing that ~20% of rework lacked proper MES documentation, leading to miscommunication and redundant rework.
Vent Hood Airflow Study
- Investigated glycerin drip issues at AMEC 19 by analyzing airflow dynamics and thermal conditions across multiple AMEC generations (GEN 1–3).
- Collected and analyzed quantitative data measuring: Airflow rates at 6" ducts (avg. 667–1,376 fpm) Surface temperatures across vent hood components (front, rear plenum, scrim, ductwork).
- Created structured spreadsheets to log and compare airflow and temperature data across GEN 1–3 AMEC units.
- Identified potential causes of front-drip accumulation, including suboptimal airflow distribution and dew point differentials between fabrication and membrane environments.
- Recommended vent hood redesigns to improve airflow and eliminate condensation zones.